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"True"
Horizontal Tin Can Stirling Engine
 Most tin can engines either have their displacer piston and power piston in the vertical posision.
Or as in the walking beam tin can it has one in the vertical posision (displacer piston) and one in the horizontal posision (power piston).
This is the first tin can engine to place both the displacer piston and power piston in the horizontal posision.
Making it a "true" horizontal tin can stirling engine.

Disclaimer (sort of )
I would build the "Walking Beam Stirling Tin Can Engine" first if this is your first engine. There is more details and hints that are very helpful to the first time tin can builder. 

If you have already build a working , then you will be able to figure out how to build this one. Close to the same as the "Walking Beam Stirling Tin Can Engine" with a few major changes. You're on your own!!


 

This projected started with a "Walking Beam" engine displacer cylinder ,power cylinder,
and displacer I started and decided not to finish. Instead I decided to make a "true" Horizontal engine out of it.
 


Reworked displacer piston. Note rod is steel not brass and
goes through the displacer and out the bottom 5 1/2".
Brass rod sags too much and a steal rod eliminated this problem.
 
 
 
 


View of top bearing of Displacer Cylinder.
Same as the original "Walking Beam" engine.
 
 
 
 


Reworked displacer cylinder. Note brass tubing silver soldered onto
the bottom to help support the displacer piston.
(This is not the finished design. See below)
 
 
 
 


Displacer piston is slid into the displacer cylinder and top is then added
(This is not the finished design. See below)
 
 
 
 


Top is then soldered on
(This is not the finished design. See below)
 
 

Changes !!!

After some consideration, I decided to make a few changes.

1) On the bottom or to the left I removed the brass tube and replaced
it with a brass bolt with a 1/8" hole down the middle just like the top bearing. I was concerned with the extreme heat melting the solder and releasing the brass tube bearing. This "bolt-in" approach removes this possibility.

2) I made a temporary brace to help hold the power cylinder straight and true while soldering. I wired this on.
 
 


 


Temporary brace and wires were then removed.
 
 
 


Displacer cylinder was installed and top was soldered on.
Painted with high temperature black paint.
 
 
 
 


Another good photo of the "new" bottom bearing.
 
 
 
 
 


Good photo of the top bearing. Same as the "Walking Beam" Engine.


Phase 2

horizontal stirling_01
Some alterations were made.
The old copper pipe was removed and a new style power cylinder and piston was installed
.You can see the new style cylinder here


horizontal stirling_02
I added a 90 degree elbow fitting to the back of the new cylinder

The water cooler tin can was hole sawed out and fitted on the displacer.
Then it was attached using red hi temp silicone sealer. You can get this at any auto parts store


horizontal stirling_03
I used a U bolt from Orchard Hardware for mounting front and back.
Copupling nuts at the bottom with flat head machine screws will mount from under the wood board when mounting.



horizontal stirling_04



horizontal stirling_05



horizontal stirling_06
Picture of front U bolt setup


horizontal stirling_07
Ready to mount to a board.


horizontalpase2_1.jpg
Here it is mounted to a shelf board.


horizontalpase2_2.jpg
Close up of the power piston just hanging out just a little.
I used a rod end from a hobby shop on the power piston.
Now for the fly wheel!


Phase 3

Almost done. In this phase (at the end) I fired it up. It would make about 3 to 4 cycles and then stop.
More on that later!

horizontalphase3_01.jpg
I used tie rod ends from RC planes to make the connecting rod



horizontalphase3_02.jpg


horizontalphase3_03.jpg


horizontalphase3_04.jpg

horizontalphase3_05.jpg


horizontalphase3_06.jpg
I used RC rod ends and clevises to make the displacer rods. I had to support the rod coming out of the displacer
cylinder with a brass rod. This made the rod go in and out easier without binding.

horizontalphase3_07.jpg
A better view of the same rod

horizontalphase3_08.jpg
As I said earier, I fired it up and it would go about 3 or 4 cycles and then stop. I removed
the piston rod from the flywheel crank and turned the flywheel around creating "cycles".
The piston would push out and pull in just as it should, but I feel it should have a little more power.

Problem?
I think the main problem is not enough heat getting to the rear of the displacer cylinder.
As you can see I have no "hood" around the displacer cylinder to direct the heat evenly around both
sides of the cylinder (outside). I think if I fabricated a hood it would heat more evenly. I was able
to get more power by moving the Sterno can back and forth or from side to side. This heated the engine on
both sides more, but even would be better.  (no I didn;t use the entire can of Sterno. That is an enpty can with the lid on it.
The Sterno was placed on top of that to get the fire closer to the cylinder.

The second proplem is......Tha big honking "U clamp" in the rear. I think it might be sucking up a lot of heat. Sort of like
a heat sink. I think I might move that forward all the way to the water tank as close as possible. That might help a bunch also.


Still over all. 4 cycles is not too bad for a first attempt!



Phase 4
The Final Phase?
"I've got to have more power!"


horizontalphase4_01.JPG
OK, moved the mounts (pipe clamp) forward in front of the power piston exit and made a fire box.
The fire box was made from another can (like to stay with the program) and installed.

Ran great for about 2 to 3 minutes then everything broke loose....well exploded to be exact.
You will notice the small can of sterno on the left of the photo above. That can had it's lid on
and sterno on top of it to place the fire closer inside the firebox.
Very bad idea!
After running about 2 to 3 minutes that can heated up (DUH!) and exploded. That is why the lid is off
and the fire box is turned a little sideways. Didn't even see that one coming! Can was still on fire be it almost out.


horizontalphase4_02.JPG


horizontalphase4_03.JPG





horizontalphase4_04.JPG
Notice I thoiugh about removing the cap of the water tank. I though to myself.....
better remove that cap, don't want this thing building up pressure or steam and blowing apart!
Almost had it right!



horizontalphase4_05.JPG
Firebox removed from rear of engine

Still it ran for some time there. I need to work on the timing a little and a new way to deliver the fire into the fire box.



That's it! I don't see a PHASE 5!


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